Nice but what came off at the end?
the dip stick shot out and he lost some oil.87camaroPA said:Nice but what came off at the end?
What?!?!?! Did you guys figure out how that happened? Because that is not good.nitroinsane said:the dip stick shot out and he lost some oil.
Yeah for something going wrong.CoBIZZLE said:hmm.... Still fairly ok numbers, I imagine he had to get off the throttle a lil soon though...
Yeah that may have happened it could have been over full but still.wheelburns said:how the frick does that happen? like im very very confused unless he was the guy that put in 7 qts like the others on here that say 7 i dont understand how it would happen.
he went was at 195 stock i beleive. i think he took out a headgasket he didnt even have 100 miles on the new head lolCoBIZZLE said:Yeah but we werre sayin that cuz people have been dynoin OVER 210 bone stock....Check out Modern Performance's dyno vid!
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I would surely love to watch you do that, considering the ECOTEC(including the LSJ) does NOT have a PCV Valve.DigDug said:ring blow-by, pressurized the crankcase, car probably burns quite a bit of oil (or soon will). Putting in a new PCV valve might help some.
See, told ya he knows everything.WopOnTour said:I would surely love to watch you do that, considering the ECOTEC(including the LSJ) does NOT have a PCV Valve.![]()
WopOnTour
WopOnTour said:I would surely love to watch you do that, considering the ECOTEC(including the LSJ) does NOT have a PCV Valve.![]()
WopOnTour